Elixir Energy Ltd (EXR)
Daydream 2 Impressive Initial Flow Test
5 April 2024 9:33 AM. Original PDF: Open PDF | 4 PagesElixir Energy Limited announced highly successful initial flow test results from the Daydream-2 well in Queensland, achieving a maximum flow rate of 2.3 MMSCFPD and a stabilized rate of 1.3 MMSCFPD.
Summary
- Elixir Energy Limited conducted successful flow tests at the Daydream-2 well in Queensland.
- Achieved a maximum flow rate of 2.3 MMSCFPD and a stabilized rate of 1.3 MMSCFPD.
- This is the deepest unstimulated gas flow in onshore Australia East of the Perth Basin.
- Testing was not affected by recent heavy rain, showcasing good ease of access and infrastructure.
- Plans for further stimulation to increase flow rates and additional appraisal well Daydream-3 are underway.
- Gas samples from the test have low CO2 content, indicating high quality.
Highlights
- Maximum rate: 2.3 MMSCFPD
- Stabilized rate: 1.3 MMSCFPD
- Height of flare: estimated 15 meters
- Total gas produced over both flow periods: 0.6675 MMSCF
- CO2 component: 1.6%
- Depth of tested zone: 4,200 - 4,217 meters
Positives
- Highly successful initial flow test without stimulation.
- Stabilized flow rate achieved signifies potential for significant gas production.
- The flow test indicates a potential major contribution from the Lorelle Sandstone to the project's economics.
- The project's location and infrastructure support ease of access and further development.
- Low CO2 content in gas samples indicates pipeline quality gas.
Negatives
- Only a small percentage (19%) of the total net pay will be targeted in the upcoming stimulation program.
Key Dates
- 5 April 2024: Announcement date of the successful flow test results.
Alerts
- Contains better than expected results: yes
- Contains worse than expected results: no
- Contains expected results: no
- Sentiment: positive